| '69 Stang "The Beast" |
 | October, 2009 - I found out in August
that I qualified to participate in the NHRA ET Divisionals, being held at
Firebird International Raceway in Phoenix. We went up to Phoenix on
Thursday, Oct.1st for the TnT, 2 runs, and we got one more run on Friday
and one on Saturday, which was supposed to be the day we began elimination
runs but didn't. Sunday, we had one test run on Sunday before the
first round of eliminations. Choosing your dial in was pretty
difficult, as the runs were far apart and it was cool and humid in the
morning, hot and drier in the afternoon. I won my first round, sheer
luck with choosing my dial more correctly than my opponent. I lost
the second round, by .004 and wasn't sure which of us won until I saw his
win light come on. It was fun and I hope I'm able to go again! |
 | August, 2009 - The car has been running
very well, though I've been having problems getting it to run in the
mid-12s since the clutch was replaced. A very large slam on the
bottom of the car proved to be the rear spring mounts snapping. We
took the car to Leon's Exhaust for the chassis mods and taking his
recommendation, replace he old traction bars with ladder bars and frame
stiffeners. The few times I've run it since it's been bogging off
the line, so I've raised the tire pressure and it's still bogging. I think
I may need to change my launch RPMs to 5500 to overcome this. |
 | September, 2008 - This is the first time I have EVER had to say this but
I finally broke the '69 Mustang. I had made 3 practice runs, at the
last R1320 race of the year, the first was a really good run, even though
the effective altitude was about 6600'. The next two runs, I had
trouble hitting 4th gear, though the 3rd run was pretty darn good even
missing 4th gear, I still wanted to make one more run, under the
assumption that missing 4th was driver error, not the car. On run
number 4, I had a difficultly getting the shifter into 2nd, which is the
gear I do my burnouts in. I finally did, and the burnout was fine,
but when I released the line lock button to pull out of the burnout I
heard something. I couldn't put my finger on the sound but I
pushed in the clutch and put it shifter in 1st, let out the clutch to pull
up to the lights and......nothing....I tried again, pulling it out of gear
and put it back in, still nothing. I tried reverse, and
2nd.....nothing....clutch is gone is our guess, as after we pushed it off
the track the smell of clutch about knocked us over. No worries
though, team races are done for the year and even though I'd like to race
it in the "Quartermile for a Cure" on November 1st, if I can't I race the
little Mustang (the '05). |
 | November, 2007 we changed out the tranny for a wide ratio,
which significantly improved my 60' time once I mastered the new shift point.
But before that happened we had a horrible bog off the line. The new
harder launches were causing the gas the in carburetor to slosh away from the
pick ups and the car was running out of gas. Patrick remedied the bog by
putting extenders on the jets. Then he decided he wanted to change out the
front shocks to Lakewood 90\10s. With these 3 simple changes, tranny, jet
extensions, and shocks, the new fastest run is 12.46 @ 108 mph. |
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